1958_08_06_USN_Neubig_Phil
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United States Marine Corps (Reserves) |
VMA 543 |
F9F-6 Cougar |
BuNo 13004 |
Wednesday 6th August 1958 |
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USMC Reserve Squadron D NAS Glenview |
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| 1st Lt. Philip H. Neubig | ||||
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"I didn't 'hang' long
enough to die" ___________________________________________________ Following several fatal unsuccessful ejection attempts by VMA 543 pilots who had jettisoned their aircraft's canopy the Squadron policy was to eject through the canopy. The rationale being "You'll get banged up but you'll get out." This was never more true than in the case of Marine Reservist Phil Neubig ___________________________________________________ Nearly fifty years later Phil Neubig still clearly remembers the events of the morning of Wednesday, 6th August 1958. Then a 28 year old flight engineer for United Air Lines and an active member United States Marine Corps Reserve, 1st Lieutenant Neubig was on a routine flying mission out of NAS Glenview, Illinois, USA. He was to fly a cross country IFR flight from Glenview to NAS Memphis in Tennessee. Marianne, his wife, was away from their home in Washington Street, Wheaton visiting in Alabama. Neither could have imagined the events that would unfold that day Shortly after take off the electrical compass in his aircraft, a Grumman F9F-6 Cougar, BuNo 13004, failed and Phil decided to continue the flight using a water compass since the destination could be reached within the parameters of VFR (Visual Flight Rules) Despite the weather forecast indicating a clear flight that August day Phil suddenly found conditions changing rapidly. The instrumentation not showing what Phil was experiencing He recalls, " Flew attitude with Gryro Horizon at 21,000 feet. I looked down to change the radio frequency. When back on instruments the gyro indicated wings level, the needle ball however said left turn and the air speed had dropped to 150 kt. I pushed over to pick up air speed, the air speed now was at "zero" and the warning flag on the gyro had disappeared." Phil's Cougar's engine had stalled and then entered into a spin. The air speed now picked up and the altitude wound down rapidly. Having dropped 11,000 feet Phil took a final look at the dial showing the speed, he was now at mach.95. He had no option but to eject. At 10,000 feet in definitely unfavourable circumstances he ejected himself through the plexiglas canopy. As he did so things then became a whole lot worse. Phil again. "I believe that the "D" ring and Mae West toggles caught on fragments of the shattered canopy releasing the parachute and inflating the life vest. So, when I separated from the seat the chute blossomed and the falling seat went through the parachute canopy ripping 10 of the 28 panel - symmetrically - 5 on each side of the chute and several of the shroud lines." On ejection through the canopy Phil's helmet had split in two and was later found a field along with the seat and wrapped in parachute silk. At this point other problems arose. "The inflated life vest was pushing the chest strap of the 'chute harness up under my neck."
"I had two painful rope burns on
my neck from where the helmet chinstrap had been. I was just about
strangled by the chute harness - so much so that the blood vessels in my
face had extended."
His injuries would put him in the
Great Lakes Naval Hospital, Illinois for 8 months. The farmer who witnessed the events recalled two loud bangs. Phil's actual memory of the seconds immediately having activated the ejection sequence are clear, "I last remembered hitting the rain, and the slipstream, and thinking I'd better pull the "D-Ring" in case the barometer release failed. This was impossible as both my arms were broken. (In fact he had a broken left arm and a dislocated right shoulder) and I was tumbling. The events of the next 9,500 feet did not register with Phil as he was knocked unconscious when he 'hit" the violent slipstream.
On the farm in Waterford
Wisconsin, Illinois, watching the whole episode unfold, was farmer
William Schmidt and his son James, who later described Phil's appearance
as he descended through the storm breaking out" of the overcast at 1,100
feet as a 'collapsed balloon' The remains of BuNo 13004 were scattered over the farmland and had dug a 30 foot wide crater.
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News Headlines from the Chicago Daily Tribune the following day
The 30 foot crater made by the Cougar
In 1959, a year after the mishap Phil returned to the Scmidt's farm. This time by a conventional method and personally thanked the farmer, William Schmidt, (far right) and his son, James, seen here held by the recovered Phil Neubig.
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| 6th August 1958 |
USN |
F9F-6 Cougar |
BuNo A130009 | NAS Glenview, IL | At Waterford,WI USA | Phil Neubig ejected | ||
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Parachute - #68145 type MS3R 2 gores torn out - 10 panels blown out at high speed ejection parts of the parachute were found attached to the ejection seat - seat went thru the chute when it blossomed |
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| 6th August 1958 | F9F-8B | BuNo 141172 |
NAATC Chase Field |
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